Lead Free Assembly of Chip Scale Packages
Chip scale packages (CSPs) are widely used in portable electronic products where there is also a growing trend to lead free
assembly. Many CSP designs will meet the thermal cycle or thermal shock requirements for these applications. However,
mechanical shock and bending requirements often necessitate the use of underfills to increase the mechanical strength of the
CSP-to-board connection. Three underfill options compatible with lead free assembly have been evaluated: capillary
underfill,fluxing underfill and corner bond underfill. CSPs with eutectic Sn/Pb solder were used for control samples. Without
underfill,lead free and Sn/Pb eutectic drop test results were comparable.
Capillary flow underfills,dispensed and cured after reflow,are commonly used in CSP assembly with eutectic Sn/Pb solder.
With capillary flow underfill,the drop test results were significantly better with lead free solder assembly than with Sn/Pb
eutectic.
Fluxing underfill is dispensed at the CSP site prior to CSP placement. No solder paste is printed at the site. The CSP is placed
and reflowed in a standard reflow cycle. A new fluxing underfill developed for compatibility with the higher lead free solder
reflow profiles was investigated. The fluxing underfill with lead free solder yielded the best drop test results.
Corner bond underfill is dispensed as four dots corresponding to the four corners of the CSP after solder paste print,but
before CSP placement. The corner bond material cures during the reflow cycle. It is a simpler process compared to capillary
or fluxing underfill. The drop test results with corner bond were intermediate between no underfill and capillary underfill and
similar for both lead free and Sn/Pb eutectic solder assembly.
The effect of aging on the drop test results with lead free solder and either no underfill or corner bond underfill was studied.
This test was to simulate drop performance after the product has been placed in service for some period of time. There was
degradation in the drop test results in both cases after 100 and 250 hours of storage at 125oC prior to the drop test.
The assembly processes,drop test results and failure analysis are presented.